Incident
at RED DEER REGIONAL AB (CYQF)
PLR 603, a BAe Jetstream 31 operated by Northwestern Air Lease, departed from Runway 16 at Red Deer (YQF) on an IFR flight to Fort McMurray, then the crew cancelled IFR and returned to YQF. No reason for the turnback was provided to ATC.
UPDATE Maintenance and Manufacturing reported that when training is carried out and an emergency gear selection is made/carried out, the bypass valve is tripped. Once the flight finished the crew re-sets this valve. Due to the design, the valve can look like it is re-set but not quite. Also they have noticed as the aircraft ages this happens more often. The valve is "on condition", but due to this incident, the company is going to remove this valve and send it out to be tested to see if the tripping pressure has lowered due to wear/age. If this is the case, they are going to begin a maintenance program to have the valves rotated out to be tested at a set maintenance interval (remove them from an "on condition" to a set time).
UPDATE Maintenance and Manufacturing reported that upon take off from YQF the main landing gear would not retract. The Captain cancelled the flight plan and returned to base. Upon approach to the airfield, the gear was cycled without incident. The Captain wanted to consult with maintenance and the landing was carried out without incident. After a call to NWAL?s maintenance department, it was verified that the MLG Emergency By-Pass shuttle valve had partially tripped, causing no retraction of the MLG. The valve was re-set and a ?crew only? test flight was carried out to verify maintenance actions. After an incident free test flight, the original scheduled service was carried out.